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上海电力大学学报:2017,33(6):559-562
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1 000 MW超超临界机组深度调峰研究与实践
(1.华电句容发电厂;2.上海电力学院)
Exploration and Practice of Deep Peaking of 1 000 MW Ultra Supercritical Unit
(1.Huadian Jurong Power Plant, Zhenjiang 212413, China;2.School of Energy and Mechanical Engineering, Shanghai University of Electric Power, Shanghai 200090, China)
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投稿时间:2017-09-07    
中文摘要: 华东电网节假日期间的负荷特性和日电量曲线变化幅度较大.为适应电量变化,大型火电机组深度调峰势在必行.锅炉燃料特性和最低稳燃特性是燃煤机组深度调峰的影响因素.根据华东电网调峰的要求,句容电厂对1#机组进行了深度调峰研究并开展了深度调峰实践.结果表明,1 000 MW对冲燃烧方式锅炉深度调峰期间最低稳燃负荷可以达到250 MW,同时可以保证脱硝、脱硫、除尘设备的正常运行.
中文关键词: 超超临界机组  深度调峰  锅炉  负荷
Abstract:The range of load characteristics and daily power curve of the East China Power Grid changes significantly during the holiday.In order to adapt to changes in electricity consumption,the large capacity units to participate in peak regulation is imperative.The boiler fuel characteristics and the minimum stable combustion characteristics of coal-fired unit are factors in the peak peaking.In compliance with the East China Power Grid Dispatching Center requirements,the Unit 1 in Jurong Power Plant carries out the study and practice of the depth of peaking.The results show that the 1 000 MW opposing the firing boiler under the minimum stable-combustion load can reach 250 MW.At the same time,the denitration,desulphurization and dedusting system work properly.
文章编号:20176009     中图分类号:    文献标志码:
基金项目:中国华电集团重点科技项目(CHD-KJ-2016006).
引用文本:
孙海彦,高炜,刘润华,等.1 000 MW超超临界机组深度调峰研究与实践[J].上海电力大学学报,2017,33(6):559-562.
SUN Haiyan,GAO Wei,LIU Runhua,et al.Exploration and Practice of Deep Peaking of 1 000 MW Ultra Supercritical Unit[J].Journal of Shanghai University of Electric Power,2017,33(6):559-562.